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  3. 💬 Various bootloader files based on Optiboot 6.2

💬 Various bootloader files based on Optiboot 6.2

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  • S Offline
    S Offline
    Samuel235
    Hardware Contributor
    wrote on last edited by
    #149

    Could you please either include your sketch here or give us a link to the example sketch that you used please.

    MySensors 2.1.1
    Controller - OpenHAB (Virtual Machine)
    Gateway - Arduino Mega MQTT Gateway W5100

    mar.conteM 1 Reply Last reply
    0
    • S Samuel235

      Could you please either include your sketch here or give us a link to the example sketch that you used please.

      mar.conteM Offline
      mar.conteM Offline
      mar.conte
      wrote on last edited by mar.conte
      #150

      @Samuel235
      Resolved
      I have try with sketc j gammon https://www.gammon.com.au/forum/?id=11497
      And the problem are pir input (model hrc-501)
      Are ever high and the cpu dont go in sleep.
      I have remove pir and all ok the atmega run 20 uah very good.
      Can you advise a good pir wich run to 3,3 V for my project?
      Tanks

      M.C.

      mar.conteM 1 Reply Last reply
      0
      • mar.conteM mar.conte

        @Samuel235
        Resolved
        I have try with sketc j gammon https://www.gammon.com.au/forum/?id=11497
        And the problem are pir input (model hrc-501)
        Are ever high and the cpu dont go in sleep.
        I have remove pir and all ok the atmega run 20 uah very good.
        Can you advise a good pir wich run to 3,3 V for my project?
        Tanks

        mar.conteM Offline
        mar.conteM Offline
        mar.conte
        wrote on last edited by mar.conte
        #151

        @mar.conte
        im not sure why pir with simple test like this http://playground.arduino.cc/Code/PIRsense is ok
        but with my sketch the cpu reset forever

        
        #include <Arduino.h>            // assumes Arduino IDE v1.0 or greater
        #include <avr/sleep.h>
        #include <avr/wdt.h>
        #include <avr/power.h>
        #include <avr/io.h>
                    
        
        
        ISR (PCINT2_vect)
        {
          // handle pin change interrupt for D0 to D7 here
        }  // end of PCINT2_vect
        
        
        
        const unsigned long WAIT_TIME = 4000;
        
        
         const byte  LED =8 ;
         
         const byte  LED2 =9 ;
        int  wakepin =3 ;
          unsigned long lastSleep;
        
        
        
        volatile boolean motionDetected=false;
        float batteryVolts = 5;
        char BATstr[10]; //longest battery voltage reading message = 9chars
        char sendBuf[32];
        byte sendLen;
        void checkBattery(void);
        
        #include <RFM69.h>    //get it here: https://www.github.com/lowpowerlab/rfm69
        #include <SPI.h>
        
        //*********************************************************************************************
        // *********** IMPORTANT SETTINGS - YOU MUST CHANGE/ONFIGURE TO FIT YOUR HARDWARE *************
        //*********************************************************************************************
        #define NETWORKID     100  // The same on all nodes that talk to each other
        #define NODEID        2    // The unique identifier of this node
        #define RECEIVER      1    // The recipient of packets
        
        //Match frequency to the hardware version of the radio on your Feather
        //#define FREQUENCY     RF69_433MHZ
        //#define FREQUENCY     RF69_868MHZ
        #define FREQUENCY     RF69_868MHZ
        #define ENCRYPTKEY    "sampleEncryptKey" //exactly the same 16 characters/bytes on all nodes!
        #define IS_RFM69HW   true // set to 'true' if you are using an RFM69HCW module
        
        //*********************************************************************************************
        #define SERIAL_BAUD   115200
        
        #define RFM69_CS      10
        #define RFM69_IRQ     2
        #define RFM69_IRQN    0  // Pin 2 is IRQ 0!
        #define RFM69_RST     9
        
        
        
        
        int16_t packetnum = 0;  // packet counter, we increment per xmission
        
        RFM69 radio = RFM69(RFM69_CS, RFM69_IRQ, IS_RFM69HW, RFM69_IRQN);  
        
        void setup () {
        
        
        
         
          pinMode (wakepin,INPUT);
            pinMode(LED, OUTPUT);
             pinMode(LED2, OUTPUT);
               digitalWrite(wakepin,HIGH);
           
          
          char buff[50];
         
          Serial.begin(SERIAL_BAUD);
        
          Serial.println("Arduino RFM69HCW Transmitter");
          
          // Hard Reset the RFM module
          pinMode(RFM69_RST, OUTPUT);
          digitalWrite(RFM69_RST, HIGH);
          delay(100);
          digitalWrite(RFM69_RST, LOW);
          delay(100);
        
          // Initialize radio
          radio.initialize(FREQUENCY,NODEID,NETWORKID);
          if (IS_RFM69HW) {
            radio.setHighPower();    // Only for RFM69HCW & HW!
          }
          radio.setPowerLevel(31); // power output ranges from 0 (5dBm) to 31 (20dBm)
          
          radio.encrypt(ENCRYPTKEY);
          
          pinMode(LED, OUTPUT);
          Serial.print("\nTransmitting at ");
          Serial.print(FREQUENCY==RF69_433MHZ ? 433 : FREQUENCY==RF69_868MHZ ? 868 : 915);
          Serial.println(" MHz");
        
         }
        
        
        
        
        uint16_t batteryReportCycles=0;
        
        
        
        void loop () 
        { 
            
           //rf();
        
        
          sleepNow();
           rf();
            
         //radio.sleep();
           
                        // sleep function called here 
        
        
         radio.sleep();
        }
        
        
        
        void wake ()
        {
        
         // cancel sleep as a precaution
          //sleep_disable();
          // precautionary while we do other stuff
         detachInterrupt (1);
        }  // end of wake
        
        void sleepNow()
        
        {
        
           if (millis () - lastSleep >= WAIT_TIME)
          {
            lastSleep = millis ();
        
        
            byte old_ADCSRA = ADCSRA;
            // disable ADC
            ADCSRA = 0;  
            // pin change interrupt (example for D0)
            PCMSK2 |= bit (PCINT16); // want pin 0
            PCIFR  |= bit (PCIF2);   // clear any outstanding interrupts
            PCICR  |= bit (PCIE2);   // enable pin change interrupts for D0 to D7
        
            set_sleep_mode (SLEEP_MODE_PWR_DOWN);
          
            power_adc_disable();
            power_spi_disable();
            power_timer0_disable();
            power_timer1_disable();
            power_timer2_disable();
            power_twi_disable();
          //PORTB = 0x00;
            UCSR0B &= ~bit (RXEN0);  // disable receiver
            UCSR0B &= ~bit (TXEN0);  // disable transmitter
        
            sleep_enable();
            
            noInterrupts ();
          attachInterrupt (1, wake,HIGH);
            digitalWrite (LED, LOW);
         
          interrupts ();
            sleep_cpu ();      
           digitalWrite (LED, HIGH);
        
            sleep_disable();
            power_all_enable();
         
            ADCSRA = old_ADCSRA;
            PCICR  &= ~bit (PCIE2);   // disable pin change interrupts for D0 to D7
            UCSR0B |= bit (RXEN0);  // enable receiver
            UCSR0B |= bit (TXEN0);  // enable transmitter
        
          }  // end of time to sleep
           
         
        }
        
        void rf()
        {
         char radiopacket[20] = "Hello World #";
          itoa(packetnum++, radiopacket+13, 10);
          Serial.print("Sending "); Serial.println(radiopacket);
            
          if (!radio.sendWithRetry(RECEIVER, radiopacket, strlen(radiopacket))) { //target node Id, message as string or byte array, message length
            Serial.println("OK");
        
          }
        
          radio.receiveDone(); //put radio in RX mode
          Serial.flush(); //make sure all serial data is clocked out before sleeping the MCU
          
          
        
        
         }
        

        M.C.

        1 Reply Last reply
        0
        • S Offline
          S Offline
          Samuel235
          Hardware Contributor
          wrote on last edited by
          #152

          Firstly, i can't read the structure the way you have posted your sketch. You should use the code function in the reply, the icon looks like "</>" above where you make your reply. Put your code in there for us to have any chance of reading it at all.

          Secondly, I don't think that this is the place to be posting this issue. For a start, this isn't an issue relevant to the bootloader in this thread and secondly, it doesn't even have anything to do with MySensors.

          MySensors 2.1.1
          Controller - OpenHAB (Virtual Machine)
          Gateway - Arduino Mega MQTT Gateway W5100

          mar.conteM 1 Reply Last reply
          1
          • mar.conteM mar.conte

            @alexsh1
            I have only voltmeter extec, can i mesure ua?
            Can you send simple sketch for deep sleep ?

            alexsh1A Offline
            alexsh1A Offline
            alexsh1
            wrote on last edited by
            #153

            @mar.conte yes, you can measure consumption (should be in uA) while sleeping with a good voltmeter.

            However, I really fail to understand what has Nick's sketch you mentioned to do with MySensors? I suppose some people here may be aware of sleeping issues, but again your problem has nothing to do with MySensors.

            Please see the following - it may help you troubleshoot your issue
            https://www.mysensors.org/build/battery

            1 Reply Last reply
            2
            • S Samuel235

              Firstly, i can't read the structure the way you have posted your sketch. You should use the code function in the reply, the icon looks like "</>" above where you make your reply. Put your code in there for us to have any chance of reading it at all.

              Secondly, I don't think that this is the place to be posting this issue. For a start, this isn't an issue relevant to the bootloader in this thread and secondly, it doesn't even have anything to do with MySensors.

              mar.conteM Offline
              mar.conteM Offline
              mar.conte
              wrote on last edited by
              #154

              @Samuel235
              I wanted to build my projects with mysensors, first of all I started with bootloader found in this section to try them with examples that I know because I do not know yet mysensors, I wanted to learn it so I took the liberty to insert code in your section. if you can figure out my problem thank you or I apologize for the trouble thanks

              M.C.

              1 Reply Last reply
              0
              • S Offline
                S Offline
                Samuel235
                Hardware Contributor
                wrote on last edited by
                #155

                I get why you done it, but i don't understand why. You don't need to 'know' mysensors.... There is a getting started page, i suggest you take a few hours and read through everything. I'm not helping with an issue that is completely not related to mysensors while on the mysensors forum. Just simply for future readers of this thread that come here to solve their issue, if this thread is bloated out with over 10/20 replies that is not related to the question at hand its much harder for them to find their resolution here. I suggest contacting the author of the code himself as i'm pretty sure that your issue is not the bootloader.

                MySensors 2.1.1
                Controller - OpenHAB (Virtual Machine)
                Gateway - Arduino Mega MQTT Gateway W5100

                mar.conteM 1 Reply Last reply
                0
                • S Samuel235

                  I get why you done it, but i don't understand why. You don't need to 'know' mysensors.... There is a getting started page, i suggest you take a few hours and read through everything. I'm not helping with an issue that is completely not related to mysensors while on the mysensors forum. Just simply for future readers of this thread that come here to solve their issue, if this thread is bloated out with over 10/20 replies that is not related to the question at hand its much harder for them to find their resolution here. I suggest contacting the author of the code himself as i'm pretty sure that your issue is not the bootloader.

                  mar.conteM Offline
                  mar.conteM Offline
                  mar.conte
                  wrote on last edited by
                  #156

                  @Samuel235

                  Thanks anyway, this section introduced me to some very interesting bootloader, at least with these bootloader I can get a few microamperes for my projects, I will take note of your good day and thank you tips

                  M.C.

                  1 Reply Last reply
                  0
                  • siodS Offline
                    siodS Offline
                    siod
                    wrote on last edited by
                    #157

                    Hi guys,

                    I am getting an errror when trying to burn the bootloader, any idea what´s wrong? Im using Arduino IDE 1.6.10 and these settings:
                    0_1495966865551_upload-48973443-91a2-4504-a73b-96557383d6bf

                    and that´s the error:

                    avrdude: Version 6.3, compiled on Jun 22 2016 at 16:05:21
                             Copyright (c) 2000-2005 Brian Dean, http://www.bdmicro.com/
                             Copyright (c) 2007-2014 Joerg Wunsch
                    
                             System wide configuration file is "T:\Programme\Arduino 1.6.10\hardware\tools\avr/etc/avrdude.conf"
                    
                             Using Port                    : COM10
                             Using Programmer              : stk500v1
                             Overriding Baud Rate          : 19200
                             AVR Part                      : ATmega328P
                             Chip Erase delay              : 9000 us
                             PAGEL                         : PD7
                             BS2                           : PC2
                             RESET disposition             : dedicated
                             RETRY pulse                   : SCK
                             serial program mode           : yes
                             parallel program mode         : yes
                             Timeout                       : 200
                             StabDelay                     : 100
                             CmdexeDelay                   : 25
                             SyncLoops                     : 32
                             ByteDelay                     : 0
                             PollIndex                     : 3
                             PollValue                     : 0x53
                             Memory Detail                 :
                    
                                                      Block Poll               Page                       Polled
                               Memory Type Mode Delay Size  Indx Paged  Size   Size #Pages MinW  MaxW   ReadBack
                               ----------- ---- ----- ----- ---- ------ ------ ---- ------ ----- ----- ---------
                               eeprom        65    20     4    0 no       1024    4      0  3600  3600 0xff 0xff
                               flash         65     6   128    0 yes     32768  128    256  4500  4500 0xff 0xff
                               lfuse          0     0     0    0 no          1    0      0  4500  4500 0x00 0x00
                               hfuse          0     0     0    0 no          1    0      0  4500  4500 0x00 0x00
                               efuse          0     0     0    0 no          1    0      0  4500  4500 0x00 0x00
                               lock           0     0     0    0 no          1    0      0  4500  4500 0x00 0x00
                               calibration    0     0     0    0 no          1    0      0     0     0 0x00 0x00
                               signature      0     0     0    0 no          3    0      0     0     0 0x00 0x00
                    
                             Programmer Type : STK500
                             Description     : Atmel STK500 Version 1.x firmware
                             Hardware Version: 2
                             Firmware Version: 1.18
                             Topcard         : Unknown
                             Vtarget         : 0.0 V
                             Varef           : 0.0 V
                             Oscillator      : Off
                             SCK period      : 0.1 us
                    
                    avrdude: AVR device initialized and ready to accept instructions
                    
                    Reading | ################################################## | 100% 0.06s
                    
                    avrdude: Device signature = 0x1e950f (probably m328p)
                    avrdude: erasing chip
                    avrdude: reading input file "0x3F"
                    avrdude: writing lock (1 bytes):
                    
                    Writing | ################################################## | 100% 0.03s
                    
                    avrdude: 1 bytes of lock written
                    avrdude: verifying lock memory against 0x3F:
                    avrdude: load data lock data from input file 0x3F:
                    avrdude: input file 0x3F contains 1 bytes
                    avrdude: reading on-chip lock data:
                    
                    Reading | ################################################## | 100% 0.02s
                    
                    avrdude: verifying ...
                    avrdude: 1 bytes of lock verified
                    avrdude: reading input file "0x06"
                    avrdude: writing efuse (1 bytes):
                    
                    Writing |  ***failed;  
                    ################################################## | 100% 0.16s
                    
                    avrdude: 1 bytes of efuse written
                    avrdude: verifying efuse memory against 0x06:
                    avrdude: load data efuse data from input file 0x06:
                    avrdude: input file 0x06 contains 1 bytes
                    avrdude: reading on-chip efuse data:
                    
                    Fehler beim Brennen des Bootloaders.
                    Reading | ################################################## | 100% 0.02s
                    
                    avrdude: verifying ...
                    avrdude: verification error, first mismatch at byte 0x0000
                             0xfe != 0x06
                    avrdude: verification error; content mismatch
                    
                    avrdude done.  Thank you.
                    

                    still learning...

                    alexsh1A 1 Reply Last reply
                    0
                    • siodS siod

                      Hi guys,

                      I am getting an errror when trying to burn the bootloader, any idea what´s wrong? Im using Arduino IDE 1.6.10 and these settings:
                      0_1495966865551_upload-48973443-91a2-4504-a73b-96557383d6bf

                      and that´s the error:

                      avrdude: Version 6.3, compiled on Jun 22 2016 at 16:05:21
                               Copyright (c) 2000-2005 Brian Dean, http://www.bdmicro.com/
                               Copyright (c) 2007-2014 Joerg Wunsch
                      
                               System wide configuration file is "T:\Programme\Arduino 1.6.10\hardware\tools\avr/etc/avrdude.conf"
                      
                               Using Port                    : COM10
                               Using Programmer              : stk500v1
                               Overriding Baud Rate          : 19200
                               AVR Part                      : ATmega328P
                               Chip Erase delay              : 9000 us
                               PAGEL                         : PD7
                               BS2                           : PC2
                               RESET disposition             : dedicated
                               RETRY pulse                   : SCK
                               serial program mode           : yes
                               parallel program mode         : yes
                               Timeout                       : 200
                               StabDelay                     : 100
                               CmdexeDelay                   : 25
                               SyncLoops                     : 32
                               ByteDelay                     : 0
                               PollIndex                     : 3
                               PollValue                     : 0x53
                               Memory Detail                 :
                      
                                                        Block Poll               Page                       Polled
                                 Memory Type Mode Delay Size  Indx Paged  Size   Size #Pages MinW  MaxW   ReadBack
                                 ----------- ---- ----- ----- ---- ------ ------ ---- ------ ----- ----- ---------
                                 eeprom        65    20     4    0 no       1024    4      0  3600  3600 0xff 0xff
                                 flash         65     6   128    0 yes     32768  128    256  4500  4500 0xff 0xff
                                 lfuse          0     0     0    0 no          1    0      0  4500  4500 0x00 0x00
                                 hfuse          0     0     0    0 no          1    0      0  4500  4500 0x00 0x00
                                 efuse          0     0     0    0 no          1    0      0  4500  4500 0x00 0x00
                                 lock           0     0     0    0 no          1    0      0  4500  4500 0x00 0x00
                                 calibration    0     0     0    0 no          1    0      0     0     0 0x00 0x00
                                 signature      0     0     0    0 no          3    0      0     0     0 0x00 0x00
                      
                               Programmer Type : STK500
                               Description     : Atmel STK500 Version 1.x firmware
                               Hardware Version: 2
                               Firmware Version: 1.18
                               Topcard         : Unknown
                               Vtarget         : 0.0 V
                               Varef           : 0.0 V
                               Oscillator      : Off
                               SCK period      : 0.1 us
                      
                      avrdude: AVR device initialized and ready to accept instructions
                      
                      Reading | ################################################## | 100% 0.06s
                      
                      avrdude: Device signature = 0x1e950f (probably m328p)
                      avrdude: erasing chip
                      avrdude: reading input file "0x3F"
                      avrdude: writing lock (1 bytes):
                      
                      Writing | ################################################## | 100% 0.03s
                      
                      avrdude: 1 bytes of lock written
                      avrdude: verifying lock memory against 0x3F:
                      avrdude: load data lock data from input file 0x3F:
                      avrdude: input file 0x3F contains 1 bytes
                      avrdude: reading on-chip lock data:
                      
                      Reading | ################################################## | 100% 0.02s
                      
                      avrdude: verifying ...
                      avrdude: 1 bytes of lock verified
                      avrdude: reading input file "0x06"
                      avrdude: writing efuse (1 bytes):
                      
                      Writing |  ***failed;  
                      ################################################## | 100% 0.16s
                      
                      avrdude: 1 bytes of efuse written
                      avrdude: verifying efuse memory against 0x06:
                      avrdude: load data efuse data from input file 0x06:
                      avrdude: input file 0x06 contains 1 bytes
                      avrdude: reading on-chip efuse data:
                      
                      Fehler beim Brennen des Bootloaders.
                      Reading | ################################################## | 100% 0.02s
                      
                      avrdude: verifying ...
                      avrdude: verification error, first mismatch at byte 0x0000
                               0xfe != 0x06
                      avrdude: verification error; content mismatch
                      
                      avrdude done.  Thank you.
                      
                      alexsh1A Offline
                      alexsh1A Offline
                      alexsh1
                      wrote on last edited by alexsh1
                      #158

                      @siod what board are you using? Windows or Mac?
                      I would suggest update Arduino IDE - you are running an old version

                      Many people experience similar issues when using a wrong version of IDE:

                      https://forum.arduino.cc/index.php?topic=431294.0

                      1 Reply Last reply
                      0
                      • GertSandersG Offline
                        GertSandersG Offline
                        GertSanders
                        Hardware Contributor
                        wrote on last edited by
                        #159

                        I have been using version 1.8.x (at 1.8.2 now) for quite a while now, so no experience with 1.6.10

                        Best is indeed to update the IDE, as this will also bring new versions of GCC (the compiler) and I thought also of AVRDUDE (transfertool). Not sure about that last bit though.

                        Gert

                        1 Reply Last reply
                        0
                        • siodS Offline
                          siodS Offline
                          siod
                          wrote on last edited by
                          #160

                          Hi guys,

                          thx for your quick reply. I could upload the bootloader using ver 1.6.5 of the Arduino IDE. After that I realized ther is already a 1.8.2 version released which is closing the gaps between arduino.cc and arduino.org.
                          I havent tested this version now, but I guess it was just an IDE error, so everything´s fine now...

                          still learning...

                          1 Reply Last reply
                          0
                          • M Offline
                            M Offline
                            martim
                            wrote on last edited by
                            #161

                            I have copy the file over the existing files and then I get this error with burning:

                            java.io.IOException: Cannot run program "{runtime.tools.avrdude.path}/bin/avrdude": CreateProcess error=2, The system cannot find the file specified

                            I am using Arduino IDE 1.8.2

                            1 Reply Last reply
                            0
                            • A Offline
                              A Offline
                              aclertant
                              wrote on last edited by
                              #162

                              I'm probably a rare case but I successfully burn the bootloader (atmel 328p stand alone with slimeNode board) using atmel studio7 with an AVRMK2ISP, flash the mySensors code using arduino IDE and the "nodeManager" libraries succesfully too and everythings appear properly in my HomeAssistant, very nice, I've just give a paypal tips ;o)

                              But I have no idea why I use this bootloader ??? If I used a nano, I wont change the bootloader ? Is there something better ? It could look stupid but their is no real explain about WHY I must change my bootloader on this page...

                              1 Reply Last reply
                              0
                              • R Offline
                                R Offline
                                Rolo6442u
                                wrote on last edited by Rolo6442u
                                #163

                                Found these bootloaders and using the 1MHz for some low power experiments. I did get this error message when burning the bootloader (using USBASP programmer) :
                                "avrdude: WARNING: invalid value for unused bits in fuse "efuse", should be set to 1 according to datasheet
                                This behaviour is deprecated and will result in an error in future version
                                You probably want to use 0xfd instead of 0x05 (double check with your datasheet first)."

                                The bootloader woas succesfully burned so the message was informational. I did look into this and made the following changes in boards.txt :
                                I changed all the lines containing "......bootloader.extended_fuses="
                                There are multiples sections in the file that have these lines.

                                old value -> new value
                                0x04 0xFC
                                0x05 0xFD
                                0x06 0xFE
                                0x07 0xFF

                                I used this site link text
                                for calculating the new values for the extended fuse.
                                Now the error message is gone. Maybe this is of any help when using these bootloaders.

                                1 Reply Last reply
                                0
                                • GertSandersG GertSanders

                                  @carlierd

                                  I can probably package this in a directory structure you could add to the Hardware folder in the Arduino files, but I do not have the time for it right now. I know that has been done for the original Optiboot 6.2 files already (including a pinout file for the various processor variants):
                                  https://github.com/Optiboot/optiboot

                                  For the moment I have added my boards.txt file as I use it in my Arduino IDE (common), it shows some fuse settings, but you are right: a document describing the fuse settings to use, and their effect on a bootloader would be a nice reference for many people.

                                  A Offline
                                  A Offline
                                  aramko aramko
                                  Banned
                                  wrote on last edited by mfalkvidd
                                  #164
                                  This post is deleted!
                                  1 Reply Last reply
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