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  1. Home
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  3. Motion Sensor triggering on its own

Motion Sensor triggering on its own

Scheduled Pinned Locked Moved Troubleshooting
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  • hekH Online
    hekH Online
    hek
    Admin
    wrote on last edited by
    #2

    Yes, the motion sensor actually detects heat movement. So you probably shouldn't point the motion detector against a radiator.

    1 Reply Last reply
    0
    • Matt PittsM Offline
      Matt PittsM Offline
      Matt Pitts
      wrote on last edited by
      #3

      thanks @hek the sensor is currently stuck half way up a wall, where would you recommend installing it? wall or ceiling? I was also a little unclear about the jumper settings which is best?

      1 Reply Last reply
      0
      • hekH Online
        hekH Online
        hek
        Admin
        wrote on last edited by
        #4

        On the wall, in a corner pointing into the room (away from the windows). I usually put them just below the ceiling, but it depends on your wall height.

        
        ________WINDOW___________________
        |*     RADIATOR
        | \
        |  \
        |   \
        |
        |
        |
        
        1 Reply Last reply
        0
        • bjacobseB Offline
          bjacobseB Offline
          bjacobse
          wrote on last edited by
          #5

          A tutorial how a PIR sensor is detecting, using the Fresnel lens. To understand that the PIR is detect areas of "heat" and "cold"
          http://www.instructables.com/id/PIR-Motion-Sensor-Tutorial/

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          • ErrKE Offline
            ErrKE Offline
            ErrK
            Plugin Developer
            wrote on last edited by
            #6

            I have just find out the same problem with one of my nodes that have a HC-SR501 motion sensor.
            It is a Arduino 5v with the same sketch as 3 other nodes.

            It updates every second and i have it right now in a closed box so it shuld not trigger any motion.
            I have tried to clearEEPROM and tried again, but i get the same result.

            What can i do?

            M 1 Reply Last reply
            0
            • sundberg84S Offline
              sundberg84S Offline
              sundberg84
              Hardware Contributor
              wrote on last edited by
              #7

              @ErrK try to rewire the node - you can also measure if the signal pin from motion sensor is high all the time.

              Controller: Proxmox VM - Home Assistant
              MySensors GW: Arduino Uno - W5100 Ethernet, Gw Shield Nrf24l01+ 2,4Ghz
              MySensors GW: Arduino Uno - Gw Shield RFM69, 433mhz
              RFLink GW - Arduino Mega + RFLink Shield, 433mhz

              ErrKE 1 Reply Last reply
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              • sundberg84S sundberg84

                @ErrK try to rewire the node - you can also measure if the signal pin from motion sensor is high all the time.

                ErrKE Offline
                ErrKE Offline
                ErrK
                Plugin Developer
                wrote on last edited by
                #8

                @sundberg84 thanks. I will try it.

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                • ErrKE ErrK

                  I have just find out the same problem with one of my nodes that have a HC-SR501 motion sensor.
                  It is a Arduino 5v with the same sketch as 3 other nodes.

                  It updates every second and i have it right now in a closed box so it shuld not trigger any motion.
                  I have tried to clearEEPROM and tried again, but i get the same result.

                  What can i do?

                  M Offline
                  M Offline
                  Maciej Kulawik
                  wrote on last edited by
                  #9

                  @ErrK I had similar problem with my hc-sr501 pir. It seems that some pirs are very sensitive to any electromagnetic noise. For me pir was reporting false positives each time nrf was sending data. You can easily test it: just remove any gw.send commands and solder led to pir output (of course through 1k resistor). When pir is detecting a motion output goes high so led will go on for the time set by pir potentiometer. In my case each sending (when for example battery level was reported each 30 min) resulted in false pir trigger.
                  It seems that this depends on specific device. I switched pirs between my sensors and this false triggering went to other node :-)
                  Finally I solved this problem in software. I can share my sketch that is working well for two of my nodes.

                  Btw: there are many discussions on the web about those pir false triggering concerning remote radio nodes. I took the idea of software solution from there.

                  Of course in your case reasons can be different...

                  ErrKE 1 Reply Last reply
                  1
                  • M Maciej Kulawik

                    @ErrK I had similar problem with my hc-sr501 pir. It seems that some pirs are very sensitive to any electromagnetic noise. For me pir was reporting false positives each time nrf was sending data. You can easily test it: just remove any gw.send commands and solder led to pir output (of course through 1k resistor). When pir is detecting a motion output goes high so led will go on for the time set by pir potentiometer. In my case each sending (when for example battery level was reported each 30 min) resulted in false pir trigger.
                    It seems that this depends on specific device. I switched pirs between my sensors and this false triggering went to other node :-)
                    Finally I solved this problem in software. I can share my sketch that is working well for two of my nodes.

                    Btw: there are many discussions on the web about those pir false triggering concerning remote radio nodes. I took the idea of software solution from there.

                    Of course in your case reasons can be different...

                    ErrKE Offline
                    ErrKE Offline
                    ErrK
                    Plugin Developer
                    wrote on last edited by
                    #10

                    @Maciej-Kulawik Thanks.

                    Today my second node started to do this too.
                    I have tried to change the HC-SR501 and the problem seams to be on the node and not on the sensor.
                    Can i see how you fixed this in the sketch?

                    M 1 Reply Last reply
                    0
                    • J Offline
                      J Offline
                      Jan Gatzke
                      wrote on last edited by
                      #11

                      I have solved this by reading the status of the HC-SR501 twice. Works finde for me.

                       boolean tripped = digitalRead(DIGITAL_INPUT_SENSOR) == HIGH; 
                              
                        Serial.println(tripped);
                        if (tripped==1){
                          //wait
                          delay(100);
                          //read the pin again
                          tripped = digitalRead(DIGITAL_INPUT_SENSOR) == HIGH; 
                           if (tripped==1){
                        gw.send(msg2.set(tripped?"1":"0"));  // Send tripped value to gw 
                        }
                        }
                      
                      1 Reply Last reply
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                      • R Offline
                        R Offline
                        robosensor
                        wrote on last edited by
                        #12

                        The same problem for me. Different HC-SR501 sensors (connected to one of three nodes with this sensors) periodically entering "flood mode" with continuous sending 1/0 values. I suspect that this is power supply related problems.

                        J 1 Reply Last reply
                        0
                        • bjacobseB Offline
                          bjacobseB Offline
                          bjacobse
                          wrote on last edited by
                          #13

                          I have for a sonar sensor (Ultrasonic Module HC-SR04) used in RPI and written in Python, used to measure 3 times and if all 3 measurements are same, then result is valid and data send. This is working perfect for me. You can create something similar for your Arduino

                          intdistance = 0

                                  distance = -1
                                  continueLoop = True
                                  log.debug("Loop until distance1 = distance2 = distance3")
                                  while(continueLoop):
                                      #distance = ser.read(size=3)
                                      distance = ser.readline()
                                      getValue1 =  distance.rstrip('\r\n')
                                      log.debug("distance1: %s", getValue1)
                          
                                      distance = ser.readline()
                                      getValue2 =  distance.rstrip('\r\n')
                                      log.debug("distance2: %s", getValue2)
                          
                                      distance = ser.readline()
                                      getValue3 =  distance.rstrip('\r\n')
                                      log.debug("distance3: %s", getValue3)
                          
                                      distance == getValue1
                          
                                      if  getValue1 == getValue2 and getValue2 == getValue3 :
                                          continueLoop = False
                          
                                  intdistance = int(distance)
                                  log.info("distance: %d to be sent to Agocontrol", intdistance)
                          
                          1 Reply Last reply
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                          • R robosensor

                            The same problem for me. Different HC-SR501 sensors (connected to one of three nodes with this sensors) periodically entering "flood mode" with continuous sending 1/0 values. I suspect that this is power supply related problems.

                            J Offline
                            J Offline
                            Jan Gatzke
                            wrote on last edited by
                            #14

                            @robosensor Have you tried to enable the ibternal pullup for the pin?

                            R 1 Reply Last reply
                            0
                            • J Jan Gatzke

                              @robosensor Have you tried to enable the ibternal pullup for the pin?

                              R Offline
                              R Offline
                              robosensor
                              wrote on last edited by
                              #15

                              @Jan-Gatzke said:

                              @robosensor Have you tried to enable the ibternal pullup for the pin?

                              Didn't read biss0001 datasheet, so I don't know is output pin 5V-compatible (for pullup) or not, so I didn't tried to enable internal pullup.

                              In any case I will try to check what happens with OUT pin of module during this 1/0 flood.

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                              • ErrKE Offline
                                ErrKE Offline
                                ErrK
                                Plugin Developer
                                wrote on last edited by
                                #16

                                Thanks @Jan-Gatzke it did not work for me this time.

                                I'm using a 5v Arduino Pro mini and when i measure the power on the HC-SR501 i get 3.71v.
                                When i measure the power on the VCC i get 3.69v and when i measure the RAW i get 5.43v.

                                Here you can se how everything is wired, I use the Easy/Newbie PCB by @sundberg84.
                                1_1457118103690_IMG_6345 copy.jpg
                                0_1457118103689_IMG_6346 copy.jpg

                                First i used the 5v cable to the raw on the PCB and then it did't work.
                                When I change to connect to the PWR then it works. Don't know why. Maybe @sundberg84 know why?

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                                • sundberg84S Offline
                                  sundberg84S Offline
                                  sundberg84
                                  Hardware Contributor
                                  wrote on last edited by sundberg84
                                  #17

                                  Hi @ErrK.

                                  Work your way backwards with the multimeter. Are you powering with 5v there shouldnt be a drop to 3v. Check volt over arduino and then vcc output. As i said work you way backwards in the circuit.

                                  I suspect a faulty hardware somewhere, measure the input and output on the voltage regulator on the arduino.

                                  Controller: Proxmox VM - Home Assistant
                                  MySensors GW: Arduino Uno - W5100 Ethernet, Gw Shield Nrf24l01+ 2,4Ghz
                                  MySensors GW: Arduino Uno - Gw Shield RFM69, 433mhz
                                  RFLink GW - Arduino Mega + RFLink Shield, 433mhz

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                                  • ErrKE ErrK

                                    @Maciej-Kulawik Thanks.

                                    Today my second node started to do this too.
                                    I have tried to change the HC-SR501 and the problem seams to be on the node and not on the sensor.
                                    Can i see how you fixed this in the sketch?

                                    M Offline
                                    M Offline
                                    Maciej Kulawik
                                    wrote on last edited by
                                    #18

                                    @ErrK In my case PIR switches into HIGH for some seconds (depending on potentiometer), so reading after 100ms will give the same value.

                                    @ErrK Unfortunately my solution is not 100% reliable. For 2 of my nodes it works well, but for 3rd node (the same hardware, the same sketch, only PCB is a little bi different - previous version, but difference only in dimension) - pir is false triggerring almost each minute (sometimes with 2 minutes delay with false triggering). And I checked - it is not caused by NRF sending. I have no idea whats going on.

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                                    0
                                    • rvendrameR Offline
                                      rvendrameR Offline
                                      rvendrame
                                      Hero Member
                                      wrote on last edited by
                                      #19

                                      @Maciej-Kulawik , how are you powering the node? I had once a PIR false-triggering due power instabilities...

                                      Home Assistant / Vera Plus UI7
                                      ESP8266 GW + mySensors 2.3.2
                                      Alexa / Google Home

                                      M 1 Reply Last reply
                                      0
                                      • fifipil909F Offline
                                        fifipil909F Offline
                                        fifipil909
                                        wrote on last edited by
                                        #20

                                        Hi,

                                        i'm wanted to share my experience also with those sensor.
                                        I had a lot of issue with false trigger when running on 3.3V. In my case the power was definitely the issue.
                                        it's looks like sleeping the radio/mcu cause some noise on the voltage line.

                                        I solve 100% of my false trigger issue when doing a small sleep, before enabling the sleep with interrupt.

                                        gw.sleep(500);
                                        gw.sleep(INTERRUPT,RISING, SLEEP_TIME);
                                        
                                        1 Reply Last reply
                                        0
                                        • rvendrameR rvendrame

                                          @Maciej-Kulawik , how are you powering the node? I had once a PIR false-triggering due power instabilities...

                                          M Offline
                                          M Offline
                                          Maciej Kulawik
                                          wrote on last edited by
                                          #21

                                          @rvendrame I'm powering all with 2xAA baterries. On PIR I removed regulator. The problem with false trigerring is independent from voltage level. It is the same if I put old baterries (2,8V) or brand new (3,2V).
                                          @fifipil909 I also suspect that it is somehow connected to powering noises and mcu sleeping. In my one case PIR is triggering each minute - and sleep time is also one minute.

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